Jump to content

wildebill308

Members
  • Content Count

    8135
  • Joined

  • Last visited

  • Days Won

    5

Everything posted by wildebill308

  1. I use Mobil -1 0-20 in my new Honda and I bet it would work great in your V-10. You can go to Mobil1 website for oil and filter recomendations. I am in Fort Worth and it has ben over 110 at times hear and I have no fear of my oil breaking down. Bill
  2. I have been having fun getting to know my new to me 2003 Bounder 38 ft diesel pusher. I noticed it had a FMCA number on it. I am wondering if the last owner uses the forums the number is FMCA 368494. I think it would be fun to talk to them. Bill
  3. Sam, When it runs on 2 different fuel supplies it is not out of fuel. Planocat, You are right. I was thinking it might be an over temp sensor as it was 105 that day. Well they called and told me they had to replace the radiator and it cost them $600.00. Well glad the shop made their money off them not me. I am going to go tomorrow and try to get this deal done. Thanks for all the help and comments. Bill
  4. Herman, I apologize it is a Onan 7500 quiet diesel. Wayne77590, You are right I am glad it happened on their lot not 35 feet from their door. I didn’t hear aneything today. I am going to call tomorrow. Bill
  5. Over 1/2 tank and would not run from alternate fuel supply. Bill
  6. New to this forum and thought you might like to read about my little adventure. Well I had an interesting afternoon. Saturday I went to do my final walk through and test drive on my new to me 2003 bounder 38U diesel pusher. They had it plugged into shore power when we got there. It was nice and cool inside and about 104 out side. This let us check all the systems. I was impressed with how much ice the freezer had made in a fairly short time. Everything was going just fine. We finished the outside and disconnected the shore power and started the gen to get ready for a test drive. We were waiting for a tech to put on the plates and do a minor maintenance item (the awning over the door was not moving smoothly and trying to hang up. The tech that was helping was spraying some lube on the pivot points). Well while we were setting in the nice cool coach the generator quit. Tried to restart but it ran about 5 min and quit. Tried this a couple of times. Tried checking the oil level, fuel was at ½ tank. The tech tried changing the fuel filter. Then they tried hooking up a different fuel source no luck. Interesting as we had run the generator earlier in the week when we were talking to the salesman for problem 45 min to one hour. Worked great. They are taking it to have it fixed Monday, as they don’t have any one who knows how to work on diesel generators. Well the good news is it quit in their lot before I singed the papers not on the road some place lol. Bill
×
×
  • Create New...